Back Again.
Since this receiver was obviously way off, I decided there was little point in machining to correct it. Sterner measures were called for. Some accuracy gunsmiths and shooters may find some of these methods offensive. Reader's dicretion advised!
I set up a couple of lead blocks and laid the receiver on them with the left receiver wall facing up. Using a chunk of aluminum to protect the receiver surface, I whacked it sharply with a 3 pound hammer. Just a few well placed blows had the mandrel coming through within .005" of the center of the test piece. This also served as a form of stress relief. Not on the receiver but on me! There's something about beating on a new action with a big hammer that just makes me feel good! Anyway, with things much straighter (the receiver wall was now almost perfect!) I could go ahead and set it up in my action fixture just as I would any other action. I did so.
After removing the test piece and the mandrel, I was ready to start truing. I bored out the ID of the c-ring to .812". This gave me room to get in and machine the "as cast" locking lug seats. It was during the machining of the locking lug seats that I discovered another interesting idiosyncracy of the MRC design. The locking lug recess is neither concentric nor round! On the MRC bolt, as on many others of simlilar design, the right hand locking lug (the one under the extractor), is shorter than the other by about .025" or so. This difference is reflected in the receiver. So, when you go in with the boring bar and face the lug seats until you reach the bottom, you ain't done with the top seat yet. I just rocked the spindle back and forth while advancing the tool a bit with each "rock". It worked out fine.
All the while I had been bugged by the lack of lateral support for the front of the bolt and decided to try and do something about it. I had already bored the ID of the c-ring out to .812. I faced it back about .050 just to give a little more space for my threading tool to run into. I then cut a recess another .050 deep with an OD of .937. After I faced the receiver and re-cut the threads (ended up with a major diameter of 1.024"), I made a little insert which fit into the recess and extended through the c-ring. The ID was about .700". The thickness was such that it sat .001" proud of the c-ring so the barrel (and some loc-tite) would hold it in place. I then turned the nose of the bolt so it more resembled a Mauser. The coned breech was a thing of the past. The nose of the bolt would fit into the insert and the bolt would no longer act like it was trying to crawl out of the receiver. Everything worked out pretty well.
As can be seen, it took considerably more work to "true" the MRC than it would a Model 70. So much so that the cost of such work would likely exceed the value. This was a good day's work. In addition, some of the unique problems one can run into with the MRC make me question the veracity of some who say they have trued them up.
So there it is. A complete truing job on a MRC1999. One might refer to it as "Leeper's Folly" and not be far off the mark.
In all fairness, none of the other half dozen MRC actions on which I've worked have been nearly as bad as this one. Also most owners don't even notice what, to me, seemed like real shortcomings. Regards, Bill.